Starchaser 5 British manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Starchaser Industries, Cheshire, England. The concept used a rocket powered vertical takeoff followed by a parachute descent to land. |
LB-X American manned spaceplane. Study 2004. X-Prize suborbital spaceplane concept of Kelly Space & Technology, San Bernardino, California. |
Gauchito Argentinian manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Pablo De Leon of Buenos Aires, Argentina. Reached the stage of engineering tests by 2003. |
Wild Fire Canadian manned spacecraft. Study 2004. X-Prize suborbital balloon-launched ballistic spacecraft concept of the Da Vinci Project, led by Brian Feeney of Toronto, Canada. Reached the stage of engineering tests by 2003. |
Orizont Romanian manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Aeronautics and Cosmonautics Romanian Association. Reached the stage of engineering tests by 2003. |
Canadian Arrow Canadian manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Geoff Sheerin, Toronto. Reached the stage of engineering tests by 2003. |
Black Armadillo American manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Armadillo Aerospace, Mesquite, Texas. Reached the stage of engineering tests by 2003. |
Cosmopolis 21 Russian manned spaceplane. Mock-up unveiled in 2002. On 15 March 2002 Space Adventures unveiled the mock-up of their C-21 (Cosmopolis 21) spaceplane at Zhukovskiy Air Base, Moscow. |
Mayflower American manned spaceplane. Study 2004. X-Prize suborbital seaplane-spacecraft of Advent Launch Services of Houston, Texas. Reached the stage of engineering tests by 2003. |
Eagle X-Prize American manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Vanguard Spacecraft of Bridgewater, Massachusetts. |
Crusader X American manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Micro-Space, Inc of Denver, Colorado. |
SpaceShipOne Flight 15P First private manned spaceflight. Fourth powered flight of SpaceShipOne and first flight above 100 km altitude. Spacecraft rolled 90 degrees right and left at motor ignition; attitude control lost at engine shut down; engine fairing collapsed. |
SpaceShipOne Flight 16P Fifth powered flight of Burt Rutan's SpaceShipOne and first of two flights over 100 km that needed to be accomplished in a week to win the $10 million X-Prize. Spacecraft did a series of 60 rolls during last stage of engine burn. |
SpaceShipOne Flight 17P Suborbital altitude record for a manned spaceplane Sixth powered flight of Burt Rutan's SpaceShipOne and winner of the $10 million X-Prize by becoming the second flight over 100 km within a week. |
Aurora X-Prize American manned spaceplane. Study 2004. X-Prize suborbital spaceplane concept of Fundamental Technology Systems, Orlando, Florida. |
Cosmos Mariner American manned spaceplane. Study 2004. X-Prize suborbital spaceplane concept of Lone Star Space Access, Houston, Texas. |
Kitten American manned spaceplane. Study 2004. X-Prize suborbital rocketplane concept of Kittyhawk of Oroville, Washington. |
Lucky Seven American manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Acceleration Engineering, Bath, Michigan. |
Liberator American manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of HARC, Huntsville, Alabama. |
Michelle-B American manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of TGV Rockets, Bethesda, Maryland. As of 2005, flight testing of the Michelle-B was expected to begin no earlier than 2007. |
Negev 5 Israeli manned spacecraft. Study 2004. X-Prize suborbital balloon-launched ballistic spacecraft concept of IL Aerospace Technologies (ILAT), Israel. |
Pioneer XP American manned spaceplane. Study 2004. X-Prize suborbital spaceplane concept of Pioneer Rocketplane, Solvang, California. No backing forthcoming. |
Rubicon American manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of STC. |
SabreRocket American manned spaceplane. Study 2004. X-Prize suborbital spaceplane concept of Panaero, Fairfax, Virginia. It envisioned conversion of a Sabre-40 business jet to rocket power. |
Solaris X American manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Interorbital Systems of Mojave, California. |
The Space Tourist American manned spaceplane. Study 2004. X-Prize suborbital flying saucer concept of Discraft Corporation of Portland, Oregon. |
The Green Arrow British manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of Flight Exploration of London, England. |
The Spirit of Liberty American manned spacecraft. Study 2004. X-Prize suborbital ballistic spacecraft concept of American Astronautics Corporation, Oceanside, California. |
Flight Time: 0.2 hours Pilot: Shane Copilot: Siebold. Objectives: First flight. Handling qualities assessment and basic performance evaluation. Systems evaluation. Cabin un-pressurized. Results: Un-commanded hammering auxiliary spoiler deployments after takeoff. Flight aborted to downwind for an uneventful landing. No apparent flying qualities issues noted. Auxiliary spoilers were disabled for future flights.
Flight Time: 1.5 hours Pilot: Shane Copilot: Siebold. Objectives: First flight test card repeat. Flying qualities assessment and basic performance evaluation. Avionics and pneumatic systems evaluation. Cabin un-pressurized. Results: Envelope expansion to 15,000 feet and 140 knots. Overall satisfactory stability, good control harmony and impressive performance. Heavy airframe buffet at high speeds with both sets of speed brakes deployed. "Best airplane the company has ever built"
Flight Time: 2.8 hours Pilot: Melvill Copilot: Shane. Objectives: New pilot qual eval. Envelope expansion out to 25,000 feet and 150 knots. First flight with the cabin pressurized for environmental control system tests . Results: Satisfactory handling and performance. Buffet barriers determined for inboard and outboard speed brakes. Significant window fogging experienced after cold soak at altitude.
Flight Time: 2.5 hours Pilot: Siebold Copilot: Shane. Objectives: New pilot qual eval. Envelope expansion out to 35,000 feet and 150 knots / 0.4M and 3 G's. Engine relight performance. Avionics software upgrade. Results: Experienced a rudder dead-band (poor centering) at the higher altitudes. Dihedral effect is neutral at higher speeds. Window fogging on descent. Numerous flight director attitude display resets.
Flight Time: 2.0 hours Pilot: Binnie Copilot: Shane. Objectives: New pilot qual eval. Envelope expansion out to 45,000 feet and 160 knots / 0.5M. Practice SpaceShipOne glide approaches. Effectiveness of new tail vortex generators and clipped outboard speed brakes. Results: The new VGs eliminated the high-altitude rudder dead-band. Encountered undamped rudder vibration at 25,000 feet and 160 knots during flutter envelope expansion. Engine flameout at 45,000 feet. Un-safe main gear indication for landing (a microswitch adjustment). Clipped otbd speed brake showed no change.
Flight Time: 0.9 hours Pilot: Shane Copilot: Binnie. Objectives: Evaluate rudder mass balance modifications. Effectiveness of engine bleed air heating of the fuselage aft of the cabin (first test of SpaceShipOne Nitrous heating system). Results: Rudder vibration problem resolved. Flight cut short due to suspected over-temp of aft cabin bulkhead from engine bleed air.
Flight Time: 3.0 hours Pilot: Shane Copilot: Binnie. Objectives: Completion of Flight 6 objectives. Airspeed and altitude envelope expansion, 45,000 feet / 160 knots / 0.5M Results: No structural damping issues found. Engine operation satisfactory. Some window fogging on descent. Some degradation of pneumatic actuators due to cold soaking. Insufficient dihedral effect at high speed/high altitude.
Flight Time: 1.6 hours Pilot: Melvill Copilot: Binnie. Objectives: Envelope expansion above 50,000 feet and 0.55M. Avionics software upgrade. Practice SpaceShipOne glide approaches Results: Climbed to 53,000 feet and 0.53M in Military power. Cleared the full required envelope needed for SpaceShipOne launch operations. Flying qualities at highest altitude are satisfactory and will not require dampers. Window fogging not an issue until the cabin was depressurized at 10,000 feet.
Flight Time: 2.2 hours Pilot: Binnie Copilot: Siebold. Objectives: Boost phase pilot training. Formation flying and air-to-air photography with the Proteus aircraft. Results: Adequate visibility and satisfactory flying qualities for formation flying. A photo from this flight later appeared on the cover of Aviation Week (21Apr03 issue).
Flight Time: 2.4 hours Pilot: Siebold Copilot: Binnie. Objectives: Continued engine, ECS and avionics evaluation. High-rate nose wheel steering assessment. Results: Difficulty maintaining afterburner on left engine near 50,000 feet. Improved ECS configuration showed improved resistance to fogging. Nose wheel steering gearing change about the same.
Flight Time: 2.0 hours Pilot: Binnie Copilot: Siebold. Objectives: Continued engine, ECS and avionics evaluation. Simulated wheel brake failure landing rollout. Results: Conclusion: aircraft can be landed at MHV if a wheel brake fails. More engine irregularities at high altitude. Engines removed and sent to test cell for fuel control calibration and adjustments.
Flight Time: 2.8 hours Pilot: Binnie Copilot: Melvill. Objectives: Evaluate performance of updated engines. Measure effect of new canted wingtips. Test new landing gear doors and upgraded INS hardware. Results: New and different engine irregularities at highest altitudes. Further mods are needed for adequate ECS humidity control. Canted wingtips solved the dihedral effect problem. No flying qualities issues remain.
Flight Time: 3.3 hours Pilot: Melvill Copilot: Cory Bird. Objectives: Revised ECS configuration evaluation. Multiple SFO (simulated flame out) approaches to assess updated flight director steering cues. Results: New ECS configuration results encouraging. Engines returned to depot facility for second overhaul repair.
Starchaser Industries (Hyde, England, UK) successfully tested a bi-propellant liquid rocket engine. "The liquid oxygen/kerosene powered system generated some 2,200 kilos of thrust for 15 seconds." The tests will continue for increasingly longer periods and will eventually reach "a full 3 tonnes of thrust".
Scaled Composites (Mojave, California, USA) rolls out their X-Prize vehicle, consisting of the White Knight carrier aircraft and SpaceShipOne spaceplane. This is followed by a demonstration flight by the White Knight carrier-launch aircraft. Flight Time: 0.2 hours Pilot: Melvill Copilot: Binnie. Objectives: Formal media rollout Results: Good show for the VIP/media audience
Flight Time: 2.3 hours Pilot: Melvill Copilot: Rick Aldrich. Objectives: Engine performance at altitude. New pilot masks and ECS airflow routing. Regulated bleed air control of the aft cabin temperature (to test the capability to heat SpaceShipOne's nitrous oxidizer. Appraisal of new traffic alert system. Results: Engines showed much improved performance up to 50,000 feet. ECS changes confirmed to assure clear windows for landing. Successful bleed air heating test: good control and sufficient energy for SS1 propellant heating.
Pablo de León (Buenos Aires, Argentina tested his vehicle's life support systems, pressure suit, and environment controls using several high altitude glider flights to 30,000 feet using their space suit system. The suit also underwent several thermal tests in a cold chamber (-35 Centigrade) and external temperatures were sustained for more than 2 hours.
Objectives: First captive carry flight with mated White Knight and SpaceShipOne. Vibration and aerodynamic interface assessment. Mated handling qualities evaluation. Envelope expansion to 130 knots / Mach 0.5 above 45,000 feet. Stalls and 2/3-rudder sideslips. SpaceShipOne systems inactive, controls locked and cabin unmanned. Launch system was qualified and functional for this flight. Additional Details: here....
Flight Time: 2.2 hours Pilot: Binnie Copilot: Siebold. Objectives: First glide flight profile rehearsal / two ship checklist flow / airspace coordination / Command and Control responsibilities and handoffs. Results: Good exercise of all involved parties and agencies including the Edwards air Force Base, Joshua Control and Scaled Composites, Utility Mobile ground station.
Flight Time: 2.0 hours Pilot: Melvill Copilot: Binnie Flight Engineer: Rutan. Objectives: First glide flight profile rehearsal / two ship checklist flow / airspace coordination / Command and Control responsibilities and handoffs. First flight for Burt in the White Knight. Results: Exercised all current checklists and SpaceShipOne first flight test cards. Simulated emergencies handled successfully. Good exposure for Burt on cockpit workload / crew coordination / cabin environment and human factors for Tier-1 mission. Flew eleven practice SpaceShipOne approaches from above high key, three with simulated failed avionics and some with other emergencies and runway changes. All were successful.
Flight Time: 0.7 hours Pilot: Binnie Copilot: Siebold Flight Engineer: Stinemetze. Objectives: Pilot proficiency. First flight for SpaceShipOne lead engineer. Results: Made several simulated captive carry low sink rate landings as well as practice SpaceshipOne approaches to various runways. Good exposure for Matt Stinemetze on cockpit workload / crew coordination / cabin environment and human factors for Tier-1 mission
Flight Time: 0.5 hours Pilot: Siebold Copilot: Binnie Flight Engineer: Losey. Objectives: Pilot proficiency. First flight for SpaceShipOne crew chief. Results: Made several practice SpaceshipOne approaches using various configurations and runways. Good exposure for SS1 crewchief Steve Losey on cockpit workload / crew coordination / cabin environment and human factors for Tier-1 mission.
Starchaser Industries (Hyde, England, UK) conducted two manned capsule drop tests from a C-123K transport aircraft at an altitude of 14,000 feet over the Red Lake Drop Zone in Kingman, Arizona, in order to practice landing the reusable craft. The main purpose of the tests was to ensure that the parachute, navigation, and landing systems function properly.
Objectives: First manned captive carry flight of SpaceShipOne. A man-in-loop launch rehearsal and inflight checkout of all ship systems including flight controls and propulsion sytem plumbing. Results: Complete full up rehearsal for SS1's first glide flight, including airspace, range control, Scaled mission control, data and video TM and high and low chase platforms. Additional Details: here....
Objectives: First glide flight of SpaceShipOne. Results: The space ship was launched at 47,000 feet and 105 knots, 10 nm east of Mojave. Separation was clean and positive with no tendency to roll off or pitch bobble. An initial handling qualities evaluation was very positive, supported close correlation to the vehicle simulator and with that confidence, the first flight test cards were executed as planned. Additional Details: here....
Objectives: Same objectives as the aborted flight 31LC/04GC earlier today. Second glide flight of SpaceShipOne. Flying qualities and performance in the space ship re-entry or "feather" mode. Pilot workload and situational awareness while transitioning and handling qualities assessment when reconfigured. As a glider, stall investigation both at high and low altitude and envelope expansion out to 200 kts and 4 G's. More aggressive, lateral directional characteristics including adverse yaw, roll rate effectiveness and control, including 360 degree aileron roll, and full rudder side slips. Additional Details: here....
Objectives: Second glide flight of SpaceShipOne. Flying qualities and performance in the space ship feather mode. Pilot workload and situational awareness while transitioning and handling qualities assessment when reconfigured. As a glider, deep stall investigation both at high and low altitude and envelope expansion out to 200 kts and 4 G's. Lateral directional characteristics including adverse yaw, roll rate effectiveness and control including aileron roll and full rudder side slips. Results: The flight was aborted about 20 minutes before launch, after a GPS navigation malfunction occurred in the SpaceShip avionics system. The mated pair continued to test other systems including Spaceship fuselage heating, then returned for a mated landing.
Flight Time: 1.1 hours White Knight Pilot: Binnie Copilot: Bird SpaceShipOne Pilot: Melvill High Chase-Starship Pilot: Siebold Low Chase-Duchess Pilot: Karkow
American Astronautics completed a sub-scale LOX/RP-1-fueled technology demonstrator vehicle for their American Eagle I design. The test bed vehicle was capable of carrying an 18 kg payload to an altitude of 120 km. American Astronautics expected to conduct flights with the technology demonstrator in early 2004.
Flight Time: 2.7 hours. White Knight Pilot: Melvill. White Knight Copilot: Binnie White Knight Flt Engineer: Tighe. Objectives: SpaceShipOne approach and landing profile review Results: Evaluated a variety of different profiles to assess ease of set-up, forgiveness to off normal starts and pilot SA during the approach.
Flight Time: 2.7 hours. White Knight Pilot: Binnie. White Knight Copilot: Melvill White Knight Flt Engineer: Alsbury. Objectives: SpaceShipOne approach and landing profile review Results: Evaluated a variety of different profiles to assess ease of set-up, forgiveness to off normal starts and pilot SA during the approach.
Flight Time: 2.1 hours. White Knight Pilot: Siebold. White Knight Copilot: Binnie White Knight Flt Engineer: Nichols. Objectives: SpaceShipOne approach and landing profile review Results: Evaluated a variety of different profiles to assess ease of set-up, forgiveness to off normal starts and pilot situation awareness during the approach.
Objectives: Third glide flight of SpaceShipOne. Aft CG flying qualities and performance evaluation of the space ship in both the glide and re-entry or "feather" mode. Glide envelope expansion to 95% airspeed, 100% alpha and beta and 70% loadfactor. More aggressive post stall maneuvering and spin control as a glider and while feathered. Nitrous temperature control during climb to altitude and performance of upgraded landing gear extension mechanism and space-worthy gear doors. Additional Details: here....
Objectives: Fourth glide flight of SpaceShipOne. Primary purpose was to examine the effects of horizontal tail modifications at both forward and mid-range CG locations (obtained by dumping water from an aft ballast tank between test points). The tail modifications included a fixed strake bonded to the tail boom in front of the stabilator and a span-wise flow fence mounted on the leading edge of each stab at mid-span. Additional Details: here....
Flight Time: 1.5 hours. White Knight Pilot: Siebold. White Knight Copilot: Binnie. Objectives: Avionics upgrade evaluation and landing pattern practice. Results: Satisfactory GPS-aided INS stability and position keeping through a normal launch and glide flight profile. Flight 36
Objectives: The fifth glide flight of SpaceShipOne. New pilot checkout flight. Stability and control testing with the new extended horizontal tails. Tests included stall performance at aft limit CG and evaluation of the increased pitch and roll control authority. Other objectives included additional testing of the motor controller (MCS) and handling qualities in feathered flight. Results: Launch conditions were 47,300 feet and 115 knots. Satisfactory stability and control at aft limit CG. A notable improvement in control power, particularly in roll. Handling qualities into and out of feather remained excellent with good nose pointing ability. Adjusted landing pattern altitudes resulted in a touchdown at the targeted runway aim-point.
Flight Time: 1.4 hours / 19 mins 55 secs White Knight Pilot: Binnie White Knight Copilot: Stinemetze White Knight Flt Engineer: SpaceShipOne Pilot: Siebold High Chase-Starship Pilot: Karkow Low Chase-Duchess Pilot: Melvill/ Coleman
Objectives: The sixth glide flight of SpaceShipOne. Test pilot Mike Melvill's first flight with the enlarged tails. Emergency aft CG handling qualities eval and simulated landing exercise with the new tail configuration. Airspeed and G envelop expansion and dynamic feather evaluation. Additional Details: here....
Objectives: The seventh glide flight of SpaceShipOne and new pilot check out. Full functional check of the propulsion system by cold flowing nitrous oxide. Completed airspeed and positive and negative G-envelope expansion. Results: Launch conditions were 48,400 feet and 115 knots. All propulsion components, displays and functionality performed as designed. The feather was extended after a 4G pull-up to the vertical at 24,500 feet and rudder used to induce sideslip and yaw rates while "going-over-the-top". The vehicle recovered to a stable attitude and descent after only a single oscillation. The landing pattern was flown following established procedures resulting in a satisfactory touchdown.
Flight Time: 1.3 hours / 13 mins 14 secs White Knight Pilot: Siebold White Knight Copilot: Stinemetz White Knight Flt Engineer: SpaceShipOne Pilot: Binnie High Chase-Starship Pilot: Karkow Low Chase-Extra Pilot: Melvill / Coleman
White Knight/SpaceShipOne Flight 43L / 11P. Eighth flight of SpaceShipOne and first powered flight. 15 second burn of the rocket motor and supersonic flight. Motor light off at altitude and inflight engine performance. Vehicle handling qualities through transonics and feather performance from altitude. Launch conditions were 14.6 km and 207 kph. Motor light off was achieved at 13.5 km and 0.55M. Burnout occurred at 1.2M and apogee was 20.7 km. There was no noted flight control flutter or buzz during the climb. Feather recovery exhibited a +/-30 roll initially and then settled down into the familiar falling bathtub mode. The wing was de-feathered and locked by 10.6 km. A nominal landing pattern was flown but touchdown caused the left main gear to collapse and the vehicle rolled to a stop off the runway in the soft sand. Although the damage was not major, repairs were expected to take approximately three weeks to complete.
Objectives: The twelfth flight of SpaceShipOne. Objectives included: pilot proficiency, reaction control system functionality check and stability and control and performance of the vehicle with the airframe thermal protection system installed. This was an unpowered glide test. Results: Launch conditions were 48,500 feet and 125 knots. All systems performed as expected and the vehicle landed successfully while demonstrating the maximum cross wind landing capability.
Flight Time: 1.3 hours / 18 mins 30 secs White Knight Pilot: Binnie White Knight Copilot: Stinemetze White Knight Flt Engineer: SpaceShipOne Pilot: Siebold High Chase-Starship Pilot: Karkow Low Chase-Extra Pilot: Melvill / Coleman
White Knight/SpaceShipOne Flight 53L / 13P. 40 second motor burn time. Handling qualities during boost, through transonic and supersonic. Reaction control system functionality in-flight and feather configuration stability during transonic re-entry. Evaluation of radar tracking capability. Launch conditions were 13.96 km and 230 kph. A planned immediate motor ignition was delayed about 2 minutes to evaluate a shock induced stall buffet resulting in an ignition altitude of only 11.7 km. The 40 second rocket boost was smooth with good control. Pilot commented that the motor was surprisingly quiet; however the boost was heard by ground observers. Burnout occurred at 1.6M and apogee was over 32 km. There was no noted flight control flutter or buzz during the climb. Feather recovery was nominal. Maximum feathered speed on entry was 0.9 Mach. The wing was de-feathered and locked by 12 km. Handling quality assessments during descent were satisfactory and a smooth landing made to runway 30 at Mojave. All video and tracking systems performed well with spectacular footage obtained onboard, from chase and from ground stations.
White Knight/SpaceShipOne Flight 56L / 14P. 55 second motor burn time. Handling qualities during boost and performance verification. Reaction control system use for reorientation to entry attitude. Supersonic feather stability and control. Launch conditions were 14 km and 220 kph. Motor light off occurred 10 seconds after release and the vehicle boosted smoothly to 46 km and Mach 2.5. Subsequent coast to apogee of 64.5 km. During a portion of the boost, the flight director display was inoperative, however the pilot continued the planned trajectory referencing the external horizon. Reaction control authority was as predicted and the vehicle recovered in feather experiencing 1.9M and 3.5G's. Feather oscillations were actively damped by the pilot and the wing was de-feathered starting at 17 km. The onboard avionics was re-booted and a smooth and uneventful landing made to Mojave.